I finally received my Coax and the Forster Micrometer seating die. I cleaned the die and loaded about 5 rds. Runnout was about 2 thousandths. So I decided to adjust the seating stem alot higher in the die, My theory was that it would allow more travel distance for the sleeve to guide the bullet to the stem. Loaded another 5rds and cut it down to about 1 thousandths.
Some rds almost had zero runnout. I was surprised that forster didnt list this in there instructions.
I did notice that I do have some rubbing on the edges of the bullets 168smks, anyone here had any experience with Forster polishing the sleeve or the stem to fit a specific bullet?
Some rds almost had zero runnout. I was surprised that forster didnt list this in there instructions.
I did notice that I do have some rubbing on the edges of the bullets 168smks, anyone here had any experience with Forster polishing the sleeve or the stem to fit a specific bullet?